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hey guys,
Some of you may remember the trans problem i had with my rm125 (i.e. here) or so i thought it was a trans problem. Thanks to everyone who helped me solve it. Paul e.d you were right. pilot jet one size smaller was the answer.
Finally got it home today took about a dozen kick and she fired. Pulled the clutch, kicked it into first, and holy mother of tom cruise, it pulled away nice and easy. No sputtering, no stalling no nothing. just smooooooth. man im so happy. Thanks again to everyone who helped out.
Tuono
cool paul. im just happy its running nice again. Im home for the week so we'll see if it sells this week before i go back to rochester. i got a few bites on it so we'll see. If not then i'll do some more tuning when i go back.
Tuono